On September 4, 2021 the oil was changed on the 280z. As with all of my older engines, I split the oil filter open and checked for any metal particles on the filer media. Thankfully there were none.
Saturday, September 4, 2021
Monday, March 1, 2021
Fuel Rail and Injectors
I noticed that the hose connecting the sections of the fuel rail was starting to crack. The previous owner had replaced the injectors although I wasn't sure about the seals so I used this as an opportunity to inspect, clean up and replace the rubber on the fuel delivery components in the engine bay.
Wednesday, April 29, 2020
Restoring Misc Cooling Bits
Many brackets and tubes in the engine bay are showing their age. In April of 2020 I took the opportunity to address the heater hose brackets, auxiliary air valve water block and the coolant passages that feed the water block. As a bonus, I also cleaned up the engine lift bracket as well. For all the metal pieces I used a wire brush to take them to bare metal then used Rustoleum Metallic Paint & Primer in a champaign mist color to coat the parts. I've found that this paint both closely matches the cadmium zinc plating on the original parts but also holds up well in the engine bay.
Engine hoist bracket and water outlet |
Water block tubing Water Block |
Tuesday, April 28, 2020
Dealing with the Isolation
Sunday, March 15, 2020
No longer clicked off
First, I noticed that my voltage seemed higher than normal when the RPM's were above 2500 RPM.
When seeing the higher voltage my mind immediately thought of the voltage regulator. When testing the voltage with a multimeter, I found that the voltage was reading as high as 15.6v when revving. This is high by today's standards but for older cars this high of a voltage was not uncommon. Even though I never took an official reading before, I decided to change the voltage regulator anyway since I already had a new one that I purchased when Black Dragon Auto was going out of business. This unit was similar to the OE unit although it did seem to have a lesser build quality (OE on the right).
One thing I noticed right away is that one of the contacts was stuck closed on the Black Dragon unit; had I not taken the time to open the unit I would have never known this.
I also took the time to clean up all contacts at the alternator since they had years of corrosion built up.
After installing the Black Dragon unit into the car I noticed slightly lower voltage but it still bothered me that it would run in the 15v range. I did some reading and found that this was common on the cheaper regulators and found that there was a particular regulator that seemed to be recommended from Intermotor.
Internally this regulator seemed to have an identical construction to the OE regulator I removed. I installed the new regulator and also ran a ground wire from the chassis ground directly to the base of the regulator to ensure that the unit received a good ground.
In addition to the new regulator, I also read that the intermittent clicking from the electronic flasher relay can sometimes be caused by current leakage in the car wiring. This minimal current would not be enough to generate the heat required to cause the disruption in the old bi-metal flasher. While this clicking in the electronic units is common when searching for the problem, not many people have found a solution. In my research I found one customer response from the manufacturer of my flasher on the Amazon Q&A section which recommended a small resistor between the hot and the load terminals of the flasher. No other details were given but this made sense for a solution since the units "detect" engagement of the flasher by sensing ground. I tested this by creating a jumper harness with a resistor across the leads. I used a 1k Ohm 1/4 watt resistor.
This harness eliminated the "ghost clicking" when the signals were not engaged and all lights worked perfectly except for the dash indicators which dimmed and brightened instead of flashing on and off. I probably would have left it this way if I weren't already planning on making a more permanent solution. I purchased a Dorman flasher socket pigtail with the intent of making this permanent solution.
I wanted to use a resistor with a higher resistance but still 1/4 watt of capacity. The next resistance value I had on-hand was 4.1k ohms. Since this was all trial and error, why not give this one a go. I created a new harness using this resistor that would plug-in to the existing female spade connectors in the old harness.
While the electronic flasher I used would work even if the leads were swapped, I wanted to make sure the harness matched in the event that another flasher was used in the future.
I then removed the terminals from the old flasher socket and connected the new harness, using heat-shrink tubing over the connections.
So what was the result of all this work? My voltage now stays very consistent at just over 14v no matter what the engine RPM and I have a flasher that no longer clicks when the turn signals are not engaged. If I were to do it over again I would have used a resistor around 2k ohms as my flasher clicks one extra time after the turn signals are disengaged; this is still a very minor nuance that is still much better than previous behavior.
Sunday, February 2, 2020
Pure Energy
This time I installed a new coil. Why? I have been chasing an irregular miss while the engine warms up. Coils are cheap and the one on my car looked to be the original so why not give a new one a shot? Yes, yes, I know what you are saying: don't just swap parts but rather diagnose the problem. For me this is an easy way to see if the problem changes or best case goes away. It also gives me a chance to clean up some crusty terminals and nasty looking brackets.
